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1、<p> 在薩爾茨吉特有限公司修改和改造轉爐容器B </p><p> 自從薩爾茨吉特有限公司在2007年4月委命其新的轉爐B以來,該轉爐的能力增加了20 %以上。新的容器發(fā)生顯著的改善,包括滑移量的減少,更長的壽命和更高的產量。 </p><p> 在生產過程的進行中更換轉爐容器</p><p> 30多年后,薩爾茨吉特有限公司的綜合鋼廠高爐B于
2、2007年3月關閉,目的是替換轉爐B的容器,即安裝一個幫助滿足鋼鐵生產效率的容器。 該容器不得不改變自1976年發(fā)現因高的熱負荷引起的應力變形.這新的容器更大并且與懸掛系統(tǒng)結合運行,現在已展示了平靜的多的吹氧進程,而且已經實現其他的積極影響。 這篇文章論述了如期完成的成功的改造和吹氧進程的最初結果。薩爾茨吉特有限公司 薩爾茨吉特在薩爾茨吉特集團是最大的鋼鐵子公司,在其薩爾茨吉特,產約四百六十萬噸的鋼。平板產
3、品的最重要的客戶是鋼鐵貿易公司,汽車制造商和他們的供應商以及冷輥和標準大直徑鋼管的制造商,建筑行業(yè)。綜合鋼鐵廠生產從0.4至25毫米不等厚度,寬達到一千八百五十毫米的熱軋帶鋼,冷軋薄板和表面成品。生產項目包括繪畫,深沖和細粒鋼,以及高強度鋼。 大約25 %的薩爾茨吉特鋼鐵產量交付其在阿爾神伯格的寬厚板軋機作為主要材料。在這個廠,板材厚度達130毫米,寬度高達3300毫米。大約5 % 的板塊在派納重梁軋機廠被用作原料。薩爾茨吉特
4、有限公司的氧氣煉鋼廠的每年輸出能力大約是5百萬噸粗鋼。三個轉爐每天平均產</p><p> 國際大地測量公司和萬能(德國)公司生產這種設備。耳軸引腳焊接需要特殊的技術.這份工作由32名電焊工16天內不間斷的輪流執(zhí)行。 總共四部分的轉爐容器被審查安裝和全面調查。尺寸如下: ?頂端部分:7740mm,高度約2640mm ,體重約40噸; ?中間部分:7780mm,高度約900mm ,重量約16 噸; ?中間
5、部分:7740mm,高度約3610mm ,重量約49噸; ?底部:7740mm,高度約2680mm ,重量約40噸。 基于這,轉爐容器部分為了裝運和隨后安裝被安裝到指定位置。這批貨物是后勤挑戰(zhàn):一夜之間從制造業(yè)房地港奧斯納布呂克,用船運到港口,再通過幾個拖拉機拖車運到煉鋼廠 。 裝配和安裝 除了為工程所做的艱巨的設計和掌握材料的的任務外,為規(guī)劃個人裝配和安裝的步驟以期實現在最短時間內安裝需要一個全新的辦法。常規(guī)程
6、序的轉爐拆卸、裝配和安裝,最終留給德瑪格公司一個新的概念去開發(fā)。裝配和急救設備已經安裝在工廠,以求在工地快速和安全地調整組成部分。 在煉鋼廠的安裝由被承包者魏瑪有限公司(薩摩亞)正常操作 。對安裝工作進行具體調整,以適應在工廠的空間條件</p><p> 新設備的安裝 安裝碼頭的選擇,例如,該轉爐容器可以安裝在靠近海灣地區(qū)的起重機附近。沿著整個海灣繼用海灣起重機縱向運輸,該轉爐容器在轉移,提升和轉向裝
7、置上定位。此設備被用來將轉爐容器精確到毫米地插入圍墻,。一旦轉爐容器被完全定位并在其最終的位置存放,該轉爐容器齒輪組合就被安裝。最后階段的工作開始,其中包括越來越多的剩余渣裙,干擾和耐火襯里的檢查,卸載一部分的安裝。相反,該平臺,沒有任何疑慮的,順利地運行,試運行之后接著調查并研究槍的位置。隨后的時間來加熱,管理;在32天之后發(fā)起第一次吹氧進程來進行加熱,。 新轉爐的運行情況 下面是過去三個轉爐容器系列的老轉爐與最初的三新轉
8、爐容器系列的新轉爐的對比?;跈z測氧氣流量和爐渣數額的轉爐的水浸情況(見圖6 ),在薩爾茨吉特的轉爐具體要求是體積約1立方米/噸鋼。這由于結構性條件而無法實現。然而,有可能接近最佳條件,以及具體的數量可能增加到0.68立方米/噸至0.83立方米/噸。這顯然增強的水浸條件也給期望一個相應的生產參數的改進一個理由。 </p><p><b> 氧槍 </b></p>&l
9、t;p> 較大的轉爐容器減緩了氧槍噴頭的形成。許多分析中被證明,與其他兩個轉爐相比轉爐B的氧槍有更長的使用壽命: ?舊轉爐B: 168單位熱量。 ?新的轉爐B: 212單位熱量。 相較于這些價值觀念,135立方米左右的轉爐A和C的氧槍壽命是100單位的熱量 。截至2008年1月5日轉爐B 氧槍的最長壽命是445單位熱量。 冶金 在熱量的均一化的基礎上,推斷在爐渣中鐵的損失更穩(wěn)定的狀況。隨著轉爐
10、的老化,鐵在爐渣中的價值會更好這一趨勢在過去的好幾種情況下被確認。縱觀轉爐的前三個系列,它顯示出即使氧氣流量一直在增加,它也有可能減少0.1 %的鐵的含量,這相當程度地降低了吹氧時間。</p><p><b> 耐火壽命</b></p><p> 在轉爐容器中更好的冶金條件也會導致耐火材料的壽命增長。盡管由于容器的體積較大而導致耐火材料的絕對成本較高,但有可能降低
11、具體耐火材料的成本(磚和內修補混合)的7 % 。 回收轉爐廢氣 另一個積極的影響是已實現回收轉爐廢氣:它有可能增加回收的廢氣里CO平均含量的4.4 % ,而每單位熱量回收的氣體流量保持不變?;厥諝怏w的質量得到改善。 總結 薩爾茨吉特有限公司煉鋼廠的改造帶來了更符合鋼鐵生產嚴格的要求的轉爐B。該轉爐已利用試用和測試板懸掛系統(tǒng)來適用有關的熱負荷的進程;進行了轉爐容器和耳軸環(huán)合理的間隙的設計;并采用高品位,耐熱性,細粒度
12、結構鋼材。越來越大的空間已被最好方式利用,這就是為什么有可能擴大轉爐容器的大小,以至最大,與過去設計概念相比,大大增加轉換量。 利用特種車輛和適當的液壓升降,旋轉,移動設備,包括拆除和重新順利安裝一個平臺的組成部分的一種新型的裝配和安裝的概念被落實。這減少了這個尺寸的轉爐容器典型的調整時間,準確的轉爐和耳軸環(huán)力矩平衡已經允許現有的轉爐容器驅動部件的重復使用。 新的轉爐的吹氧過程只比以前更平靜,吹氧時間減少了,耐火材料和氧槍
13、的</p><p> Modification and Revamp of BOF Converter B at Salzgitter Flachstahl GmbH</p><p> When Salzgitter flachstahl commissioned its new converter B in April 2007,the converter capacity incr
14、eased by more than 20%. The new vessel geometry led to significant improvements,including less slopping,longer lining lifetime and higher yields.</p><p> Replacement of the converter vessel during ongoing p
15、roduction</p><p> The shutdown of blast furnace B in the integrated steel mill of Salzgitter Flachstahl GmbH in March 2007 was utilized to replace the vessel of converter B after more than 30 yeas, and henc
16、e to install a vessel that helps meet the requirements of efficient steel production. </p><p> The vessel that helps had to be changed dated from 1976 and showed deformations from the stress of the high the
17、rmal loads.the new vessel,which is larger and operates in conjunction with lamella suspension system,has demonstrated that the blowing process is much calmer now and that other positive effects have been achieved.</p&
18、gt;<p> The paper deals with successful modification,which was completed on schedule,and the first results of the blowing process.</p><p> Salzgitter Flachstahl GmbH </p><p> Salzgitte
19、r Flachstahl is the largest steel subsidiary in the Salzgitter Group, with an output of approximately 4.6 million tons of steel at its Salzgitter location.</p><p> The most important customers of the flat r
20、olled products are steel trading companies, vehicle and their suppliers, cold rollers , manufacturers of both standard and large-diameter tubes,and the building industry. The integrated iron and steel works produces hot
21、rolled strip, cold rolled sheet, and surface-finished products ranging in thickness from 0.4 to 25 mm and up to 1850 mm wide. The production program includes drawing, deep-drawing and fine-grained steels, as well as high
22、 –strength steels.</p><p> Approximately 25% of Salzgitter's steel production output is delivered as primary material to its heavy plate mill at Ilsenburg. In this mill, plates up to 130mm thick and up
23、to 3300mm wide are rolled. Approximately 5% of these plates are used as feedstock for rolling beams in the Peine heavy beam mill.</p><p> The oxygen steelmaking plant of Salzgitter Flachstahl GmbH has an ou
24、tput capacity of approximately 5.0 million tons of crude steel per year. The three converters produce an average of 65 heats per day with a tap weight of 210 tons per heat.</p><p> Overview of the Oxygen St
25、eelmaking Plant</p><p> The identical converters A and C were in operation since 1978 and 1977,respectively,and had already been replaced by SMS Demag in 1999 and 2000.Converter B, which remained to be rene
26、wed, was in use since 1976,producing more than 200000 heats.</p><p> This converter was subjected to high thermal loads and, as a result of the stresses involved, it showed deformations. Over the years, the
27、 cylindrical section of the converter shell had become so deformed that is nearly touched the trunnion ring at some locations.</p><p> The resulting reduction of the clearance between converter vessel and t
28、runnion ring decreased the cooling effect. For this reason, it was decided to replace converter vessel B after more than 30 years of production.</p><p> The following benefits were expected from the convert
29、er replacement and the concurrent increase in converter volume:</p><p> ·Less slopping, and less cleaning required.</p><p> ·Fewer lance skulls/longer life of the lances.</p>
30、<p> ·Less iron in the slag.</p><p> ·Improved converter offgas quality.</p><p> ·Longer refractory durability.</p><p> Requirements to Be Satisfied by the D
31、esign Concept</p><p> For the execution, a design concept was developed that aimed to increase the converter volume to the maximum possible extent and to reuse the converter drive and existing steel structu
32、res.</p><p> The scheduled period of time to perform the modification for the mechanical revamp was 30 days at the most. In the end, the modification took only 26 days. The contract was awarded to SMS Demag
33、, which has established the concept in detail and implemented it. The solution was an entirely new design of the converter from the point of view of view of suitability of the vessel for operation at high temperatures.&l
34、t;/p><p> It was possible to reuse the existing converter drive assembly. The existing free space was utilized in an optimum manner to enlarge the specific converter volume. For the vessel and trunnion ring, a
35、 high-grade, heat-resistant, fine-grained structural steel was used. The converter components were designed to be mostly maintenance-free or to require only low maintenance.</p><p> Experience that had been
36、 acquired with the old converter vessel was taken into account during the design of the trunnion ring and in determining the clearance.</p><p> The latest generation of the lamella suspension system, which
37、was developed by SMS Demag ,and the specifically adapted clearance between vessel and trunnion ring have allowed optimum natural cooling and hence axial and radial thermal expansion of the vessel. No extra cooling by air
38、 or water is required.</p><p> Manufacturing and Transport </p><p> The companies IAG and Magnum (germany) manufactured the equipment. Particular skills were demanded for welding in the trunni
39、on pins. This job was carried out without interruption by 32 welders taking turns over a period of 16 days.</p><p> The vessel in four parts was trial-assemled and entirely surveyed. The vessel in four part
40、s was trial-assembled and entirely surveyed. The vessel in four parts was trial-assembled and entirely surveyed. The dimensions are as follows:</p><p> ·Top part:7740mm,height approx.2640mm,weight appr
41、ox.40 tons.</p><p> ·Middle part :7780mm,height approx.900mm,weight approx,16 ·tons.</p><p> ·Middle part: 7740mm,height approx.3610mm,weight approx,49tons. </p><p>
42、; ·Bottom part: 7740mm,height approx.2680mm,weight approx,40tons.</p><p> Following this, the converter vessel parts were taken into assembly position for shipment and subsequent assembly. The shipmen
43、t was a logistic challenge; overnight from the manufacturing premises to the port of Osnabruck , then by ship to the port to the steelmaking plant by means of several tractor-trailers.</p><p> Assembly and
44、Installation</p><p> Apart from the demanding tasks in terms of design and materials to be mastered for the project, an entirely new approach was required for planning the individual assembly and installati
45、on steps with the aim of achieving the shortest possible installation time .The conventional procedure of converter dismounting and assembly and installation was finally left aside to develop a new concept together with
46、SMS Demag AG.</p><p> Assembly and installation aids were already fitted in the manufacturing facility in order to align the components rapidly and safely on the jobsite.</p><p> Preassembly
47、in the steelmaking plant was performed without problems by the contractor Weimarer Spezialmontagen Industrieservice GmbH (WSM).The preassembly jobs were specifically adjusted to the space conditions in the plant .These w
48、ere as follows:</p><p> ·Assembly of the complete vessel.</p><p> ·Slipping over of the trunnion ring .</p><p> ·Mounting of the vessel suspension system.</p>
49、;<p> ·Mounting of the slag skirts (main part ).</p><p> For removal and installation ,it was necessary to dismount part of the converter platform located at an elevation of 8.50 m to enable th
50、e old converter vessel to be removed on sa special shifting ,lifting and turning device .The clearance to the side walls was only a few millimeters at places .Given the space available ,the primary derives aere dismounte
51、d beforehand to allow the main gear nuit to be pulled off the trunnion pin .</p><p> The installation work was performed without any restrictions for production .Only the installation of the removed part of
52、 the platform involved a certain ristk ,as the steel structure of this platform has been in use for more than 30 years .</p><p> Installation of the New Equipment</p><p> The preassembly yard
53、was selected such that the converter ready for installation was located within the approach area of the bay crane .Following the longitudinal transport by the bay crane across the charging bay ,the converter was position
54、ed on the shifting ,lifting and turning device .This device was used to insert the converter accurately to the millimeter into the enclosure .Once the converter was exactly aligned and deposited in its final position ,th
55、e converter gear unit was fitted .</p><p> The final phase of jobs started ,which included mounting of the remaining slag skirts ,inspection for interferences and refractory lining ,and of course the instal
56、lation of the dismounted part of the platform ,which ,contrary to any misgivings ,took place smoothly.</p><p> The test run followed to survey the lance position .Then the time came for heating ,charging an
57、d launching the blowing ,process for the first heat after a total shutdown period of only 32 days ,including refractory relining .</p><p> Operating Results of the New Converter</p><p> Below
58、,the last three converter campaigns of the old converter vessel are compared with the first three campaigns of the new converter .</p><p> On the basis of the flooding conditions of a converter (see Figure
59、6)as a function of the O2 flowrate and the amount of slag ,the specific volume requirement was to be approximately 1立方米/ton steel for the converters in Salzgitter.This could not be achieved due to the structural conditio
60、ns .It has ,however ,been possible to come close to the optimum condition ,and the specific volume could be increased from 0.68立方米/ton to 0.83立方米/ton. The significantly enhanced flooding conditions have also given</p&
61、gt;<p> Blowing Lance </p><p> The larger converter vessel bowers the formation of lance skulls .It has been demonstrated in many analyses that the blowing lances of converter B have a much longer s
62、ervice life than those of the other two converters:</p><p> ·Old converter B:168 heats.</p><p> ·New converter B:612 heats.</p><p> In comparison to these values ,the l
63、ance lives of converters A and C with a volume of 135 立方米are around 100heats .The longest life of the blowing lance of converter B as of Jan.5,2008,was 445 heats .</p><p> Metallurgy</p><p> O
64、n the basis of decreased slopping and better homogenization of the heat, far more stable condition in Fe losses in the slag can be assumed. The tendency for Fe values in the slag to be better as the converter got older w
65、as confirmed in several cases in the past.</p><p> A look at the first three campaigns of converter B shows that it has been possible to reduce the Fe value by 0.1%,even while the oxygen flowrate has been i
66、ncreased. This has decreased the blowing time significantly.</p><p> Refractory Life </p><p> More favorable metallurgical conditions in the converter vessel also lead to a longer life of the
67、refractory material. Even though the absolute costs for refractories are higher due to the larger vessel volume,it has been possible to cut the specific refractory costs(bricks and inside patching mixes) by 7%.</p>
68、<p> Converter Offgas Recovery</p><p> Another positive effects has materialized for the recovery of the converter offgas: it has been possible to increase the average CO content of the recovered of
69、fgas by 4.4%,while the recovered gas flowrate per heat has remained unchanged. The quality of the recovered gas has hence been improved.</p><p><b> Summary</b></p><p> The revamp i
70、n the oxygen steelmaking plant of Salzgitter Flachstahl GmbH has brought converter B in line with the more demanding requirements of steel production. The converter has been adapted to the process-related thermal load by
71、 utilizing the tired and tested lamella suspension system;the design of an optimized clearance between trunnion ring and converter vessel;and by using high-grade,heat-resistant,fine-grained structural steels. Sufficient
72、cooling is ensured solely by the natural thermal</p><p> The mounting space has been utilized in the best possible way,which is why it has been possible to extend the converter vessel size to a maximum and
73、considerably increase the specific volume at a given tapping weight as compared with the previous design concept.</p><p> A novel assembly and installation concept,using special vehicles and suitable hydrau
74、lic lifting,turning and shifting equipment,and including the removal and smooth reinstallation of part of a platform,was implemented.</p><p> This has decreased the typical revamp time for converters of thi
75、s size. Accurate balancing of the torques of the converter and trunnion ring has allowed for the reuse of the existing converter drive assembly.</p><p> The blowing process in the new converter vessel is mu
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